Forums
New posts
Search forums
What's new
New posts
New media
New media comments
New profile posts
Latest activity
Media
New media
New comments
Search media
Members
Current visitors
New profile posts
Search profile posts
Log in
Register
What's new
Search
Search
Search titles only
By:
New posts
Search forums
Menu
Log in
Register
Install the app
Install
Forums
General Discussion
Garage
Work out of my garage/driveway
JavaScript is disabled. For a better experience, please enable JavaScript in your browser before proceeding.
You are using an out of date browser. It may not display this or other websites correctly.
You should upgrade or use an
alternative browser
.
Reply to thread
Message
<blockquote data-quote="ORVietVet" data-source="post: 22049" data-attributes="member: 9438"><p>Work on the 2002 Lexus RX300 went real quick. I had sprayed penetrant on the pcv valve threads last night. This morning it took some effort to break loose but once it did, it came right out. Installed new and reattached hose and spring clamp. The hood struts were easy peasy. Dropped one of the MAF attaching screws but I had extras in my bolt drawer. Removed air cleaner upper housing and snorkel at the throttle body and cleaned the throttle plate and bore. Reinstalled the removed components and the engine restarted no problem and road test was uneventful. The work I had done before for the CEL and 3 codes, post #72, was still good with no codes in current or history. The vehicle is done and will be picked up and paid for later today.</p></blockquote><p></p>
[QUOTE="ORVietVet, post: 22049, member: 9438"] Work on the 2002 Lexus RX300 went real quick. I had sprayed penetrant on the pcv valve threads last night. This morning it took some effort to break loose but once it did, it came right out. Installed new and reattached hose and spring clamp. The hood struts were easy peasy. Dropped one of the MAF attaching screws but I had extras in my bolt drawer. Removed air cleaner upper housing and snorkel at the throttle body and cleaned the throttle plate and bore. Reinstalled the removed components and the engine restarted no problem and road test was uneventful. The work I had done before for the CEL and 3 codes, post #72, was still good with no codes in current or history. The vehicle is done and will be picked up and paid for later today. [/QUOTE]
Verification
Post reply
Random media
Latest posts
Water intrusion in rear cargo area?
Latest: stutaeng
Today at 6:03 PM
Interior
Rebuilding 4l60e
Latest: INW-Iron-Steel
Today at 12:28 PM
Transmission & Transfer Case
4silverado's 2004 Silverado
Latest: 4silverado
Yesterday at 3:09 PM
Under Construction
2001 Tahoe high presure on low side of A/C
Latest: CPB
Yesterday at 12:45 PM
Tech Discussion
Stutaeng's 1999 Silverado
Latest: stutaeng
Thursday at 9:26 PM
Under Construction
Members online
No members online now.
Forums
General Discussion
Garage
Work out of my garage/driveway
Top